RESTORATION (1) '44 FORD GPW Frame & Body GRILL. This Ford "F" marked
grill was in relatively good condition, rusty, dented, and with twisted bars,
never the less, better than some I One dent that is causing me a problem is on the lower left front,
a 1/4" deep dent with a 1/4" bulge right smack above the same
location of a captive nut, making it near impossible to tap it out from the
rear. I'm considering drilling a hole and heating the area, and pulling the dent
up and at the same time tapping in the side. This should bring the panel back in
line. Failing that I could always remove the captive nut, panel out the dent,
and An interesting thing I've found was the left front headlight
wiring loom clip brace, broken off inside the grill edge. I measure mine as 16g,
and 1/2" to 5/8"
Staple holes for the felt were placed at random. WINDSHIELD
Having looked
around for a few years since picking up the tub which came with a slat grill w/s
frame that
Testing fit of replacement center section, Welded , and finished, no filler required. I sandblasted the inner and cut the center section away, primed the complete thing, as I could sand blast anywhere I needed to weld, filed the frame down to good rust free steel, measured what length I needed to make the replacement divider, cleaned that up and drilled out a small rust hole( shown in the top left pic) back to good steel. Using magnetic clamps , the joint was first tack welded and then after checking the alignment, a solid weld was applied, the weld was ground back, then filed to shape. The alignment was rechecked and found to be almost perfect, a little heat and the center was brought back from the 3mm error ( it was leaning back) and primed.. If you intend to do a similar repair, I can't stress enough the necessity of keeping everything in alignment and square. The next part was the Top Rail. Top Rail after sandblasting, welded up "Mirror Holes", Wiper Bushes fitted, Channel "lacework" repaired and primed. I sandblasted the top rail and what I though would be relatively
easy to repair turned out to be a little difficult, but not impossible. The
sandblasting showed up the cracks, and the rust lace work for most of the
channeling length, missing hinge rolls , split ends, extra drilled holes, it was
warped and twisted, but all original and this is what I wanted. I began with
straightening and removing the warp, then tested the fit to the outer frame
hinge, it slipped in without any problems. Next came the extra holes that had
been drilled , possibly for an inside rear view mirror, these went all the way
through, and was a simple matter of using a mig welder, grinding the weld and
filing back to shape. Next was the oversized holed that had been
drilled/gouged/worn/butchered for the wiper arm shafts, one was 3/8" and the
other was over 1/2" in diameter. I found two brass fittings with a 1/4" bore,
the right length of around 5/8", I ground off the hex head, and using a 1/4"
drill shaft rotated them on the bench grinder, this "turned" them down to 1/2"
diameter. I filed the holes in the inner to even them up, inserted the bushes
and brazed them into position, a quick grind and file and the inner started to
take on a respectable look. One end was split for about 8" from the end, I
inserted the cast corner frame brace, and inserted a shim under that to give me
clearance for paint later one. Then using the flat edge of a 1/4 x 1" flat
steel, tapped the channel fold square and even. Using the oxy I brazed
welded full length of the split and with the 4" grinder, with a new disk
attached, on edge I carefully ground
down the brazing to leave a smooth layer of brazing holding everything together.
When Sean brought up the replacement inner he included an extra top rail, so I
used this to repair the missing end hinge folds. Cutting the "new" pieces from
an old top rail, up close to the fold of the top and front edge, I filed away
the corner and fitted the new pieces, then it was a simple Friday, 26 APRIL 2002 The
ordered Glass for the Windshield arrived at 6.45pm, cut to 23" x 12.5" (x2), the
Autoglazier delivered them to the door, we test fitted to the frame, on first
inspection all appeared well, and I wrote out the cheque for AU$59.40( which
included the G.S.T. of 10%) so I was extremely pleased at the price. The
following day I checked the fit once more in the frame and found that on one
side the top rail was touching the glass which would not allow for any sealant,
my immediate thought was I had somehow made a mistake when repairing the inner
frame. After rechecking the internal measurements and the frame for square, I
then checked the glass and found that one piece was out of square, and wider on
one end than the other. On Monday I took the glass to the local glass shop where
the edge was re-ground back to square and size, retested the fit and it was
perfect, the regrind cost AU$5.... cheap!. Over the weekend I had done up a dxf
file on Monday 6 May 2002, The outer
hinge roll of the top tube of the outer frame was missing the locking tabs, also
a short TOOL BOX LOCKS Just before going over to see Al in November, I removed the
tool box l FRAME/CHASSIS There's several sections of the frame that need serious work
done, one is the Right Front Shock Mount. I
(Updated June 2009). Finally decided to tackle this job which I think is a little harder to do than the rear cross member and A-Frame I just completed. First thing was to see what I was dealing with in regards rust and available metal left on the original. Wherever possible I'll keep as much of the original parts of the frame and tub, using either reproduction or home made repair sections. I tossed out the idea of using the complete reproduction mount......Started 23 June 2009 Step 1. Seeing what I have Step 2. Separating the Reproduction Shell Halves. Step 3. Separating the Original Shell Halves What's
irking me at the moment is the repro front shock mount, the shaft is too
short when you separate the two shell halves so it doesn't fit the inner
shell of the original, ALSO........and
what's more important....is the rivet hole is in the wrong
place. Step 4. Decided to extend the shaft , remove all of the original outer bracket, including the rivet. Will now need to weld up the misaligned hole in the reproduction outer and re-drill to align with the hole in the frame. Made a riveter for my air chisel. If it works, fine, if it doesn't, I'll try something else. The riveter worked....... in a fashion....the end isn't like the Ford, too rounded, so later I may go back and try again, in the meantime, it's holding, and looks a lot better than I started with.Hole drilled for the split pin, end of the shaft tapered, Inner and Outer joined with an arc welder, so look like the same crappy welds that were there originally. I'm happy with it. This of course will be mostly covered by the battery tray when everything goes back together. - COMPLETED - 27 June 2009 - Next job:- Started 27 June 2009 is the two front frame ends, another fun job coming up! There's really one way to do this repair, remove everything from 1.125" forward of the front edge of the radiator bracket, which also aligns with 5.5" to the rear measured from the rearwar edge of the hole in the frame side. This will give me measurements for when I replace the front horns. As I wanted to re-use the
Spring Mounts, I had to cut away all the Bubba Plates, rust, excess welds,
and The next step is to fabricate
the frame horns, piece of cake! Here in Australia, it's almost I wanted to make sure the frame pieces I folded up were at the correct width, that the holes I drilled were in the correct places, that when the gussets were attached so the rivet holes aligned, that the gussets fitted within the bumper and that the whole thing was aligned so top and bottom holes in both the bumper and the gussets and the wood filler all aligned..whew!That was a mouthful.. I still need to open the large
hole in the frame repair piece and bevel back that leading edge.. Decided that as typical Ford
Pointy Head Rivets are not available I'd make my The correct length needed is the total thickness of all material the rivet will go through plus 1.5 times the diameter of the rivet. If you keep to these formulas you'll do OK for rivet diameter and length. Thanks to Bill for this information. Now that I know the ends fit the bumper and the bracket holes are in the correct position, I finished off the horns ready to be split in two. It's far easier to make these horns when the pieces are together as you have something to fit into the vise making cutting of the bottom edge easier. If you're considering making these for yourself, I've added the following photos to show how I do the cuts in this steel. The marking should be easy to see, I place the piece so I can see the marked line and then bring the disk cutter up to the line. This leaves very little to be removed after cutting. I then, using the disk cutter, grind it flat and smooth, finishing off the edges with a file . usually making the edge slightly beveled as though it were cut in a press. When making long cuts, priming the part makes for easier marking, you can see the chalk and the lines. On the photo to the bottom left, you can see where I've brought the disk up to the line, I then make a groove that the disk can run in so it doesn't go spearing off the line ruining the workpiece.Having the line visable, as you look down on the workpiece also makes for a better job. Restoration...It's all about the illusion. Once split in two, I can mark each piece where I want it to fit on each end where I cut off the old horns. I may need to make the passenger side longer as there's some pitting and old Bubba grinding grooves on what's left of the frame.
Time came around to putting everything together before riveting. I decided to scarf join the side frame rail instead of a straight weld, hopefully, this will give me greater strength as the front springs are connected to this repair section and I don't want any nasty surprises. I still need to open up the top flat of the repair piece to match the beginning of the side rail curve. While clamped and attached to the bumper so that everything fitted correctly I arc welded the pieces together, all I need do now is insert the rivets, set them, cut the frame side rail and weld everything together. It was far easier than I thought it would be. After setting the jack, my son Pat, heated the end until it was a bright red, then, using a ball pein hammer, I proceeded to form the end. As this was happening, the rivet became tighter in the hole, especially after hammering straight down with the flat of the hammer. This really is a two man job, especially when the piece is sitting loosely in the vice, there's a oxy torch going full steam ahead, and I believe it would be dangerous if tried alone. It was OK. we actually had fun, and I got to teach my son a few new words. It was late in the afternoon, so tomorrow, we'll do it all again. I couldn't get the rivets I
wanted, although a good mate sent me some from South Australia, Thanks
Mike. I'll
FRAME/CHASSIS One of the first shocks I received when I first looked at the
frame was the
Updated June 2009 Removed the offending Bubba plates, then the real shock set in, not only was the A-Frame ripped out, but the rear cross member was cracked right through. A good mate in Melbourne, Bill Mullen sent me up a section of original Ford A-Frame section, perfectly good for the purpose, all I had to do was cut out and weld in a circular section and I had the part for making the repair to the A- Frame. I had some correct gauge steel to make the missing section of the rear cross member. I asked on the Gee about a weld which
was present between the A-Frame and the rear cross member as I didn't think it
should be there. I was right and I wasn't happy about trying to grind out that
Bubba Weld.. so I took to the rear cross member with a thin cut off disk. I deliberately did rough welds when attaching the reio plate to the a-Frame and rear cross member as almost all original plates were this way. Making the reio plates was dead set easy, 20c worth of steel, one of my drawings, Rear Section - 5196-5097.gif and a 4" disk grinder and it was made in half an hour. REPAIR COMPLETED SENDER COVER As mentioned in Nabholtz, for a short period the fuel sender
cover was metal. I was fortunate to get FUEL TANK
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